HMV 904 Restoration by Hugo Holden
This set was sold to Hugo by the Early Television Museum. It is the
third of these sets we had. One of the others was restored and sold
to Tom Genova, and one remains in our collection.
This set is complete except for the CRT. Hugo plans to restore it to
working condition, and is paying particular attention to the
appearance of the finished set. Here are two sets he has restored, an
Andrea KT-E-5 and a Meissner 10-1153:

The HMV-904 Before Restoration
Here is what he had to say when he started the restoration:
March 2002: I've started on the set. It will require a complete
re-build. Most of the insulation on the hookup wire is
disintegrating, although you can still see the colours when the black
soot is cleaned off. It probably lived in a coal mining town in the
UK ! Once I've got the chassis extracted from the rest of the
components so to speak I'll be able to have it re electroplated, it
will need some glass bead blasting first to eliminate the rust. The
same for the rest of the steel metalwork. Luckily the BA thread
screws it uses are readily available new so I'll replace those with
rust free ones. All of the coils seem basically ok which is great.
I've got some rubber hookup wire much like the original to re wire it
with. Most of the resistors are ok and most of the mica caps ok but
the wax parer ones will need the treatment.
April 2002: I'm just going to replace the rivets with 6 BA nickel
plated brass screws/nuts. So I guess not original but the screws
match the history and culture. I'm not too concerned about that as
another person one day could put copper rivets in if they wanted and
you can always replace a socket more easily with screws. I've
disassembled the variable capacitor also for electroplating and
cleaning. On the sockets I can get new pins for them without undoing
the single aluminium rivet in them, as the top plate rotates so you
can get the pins out easily. I'm sticking with all the original
sockets, except for the U52(5u4) which is damaged so I'm replacing
that with a ceramic octal. I'm keeping all the original paper caps
and putting new ones inside, also the same for the leaky EHT cap,
which is a dual 0,1uF 3Kv. Like you said big job, it took a couple of
days to accurately document the wiring, especially in the rotary
switch areas!

The chassis after removal of all the components

After replating
April 2002: I've been cleaning up the yoke assembly. The center
cardboard is actually two layers of thin card. I peeled back the
internal layer to reveal wooden supports projecting through the outer
layer that I left. This increased the internal diameter by about a
1/32" or less and allows the yoke to slip over the neck of some
( but not all!) of my 5FP4 CRTs. Its an interesting yoke for sure.
The frame coils have a DC resistance of 5K! Of course the frame stage
output drives a sawtooth voltage to produce linear sawtooth current
and scan and the load is essentially resistive , however the the line
stage has 11 ohm coils and resistance is the enemy there. It relies
on the linear build-up of current in an inductor ( in the first part
of the inverted exponential curve) when a square wave is
"switched" onto it by the output stage, although inevitably
there is some resistance in the line stage load and the required
voltage needs to be trapezoidal in shape. It will be interesting to
see how this works out. I've got a new tube set and sockets coming
from the UK and and all the other bits I need like all BA thread
screws/nuts are on order. I love fixing up these old sets.
May 2002: I found that I could slice off the very end/edge of the
caps, with a very sharp new knife just as they rolled around on each
end of the cap. If you rotate the cap with one hand and hold knife
with other etc. So the total length lost was only about 0.5 to 1mm at
each end. Then I could pull out the metal end caps with the pliers by
grabbing the wire. Then warming the caps in a convection oven I could
slide out the original cap when the wax melted. The new ones were
wrapped in fibreglass tape to get a snug fit. Then the ends were
poured alternate days with polyester resin( I don't like wax because
it melts out at higher temps). The polyester resin sets a smokey
color, semi transparent. I also repaired the EHT cap, by putting a
protective tape around it, holding in the chuck of a lathe, hand
rotating and using a tool to cut a full thickness circumferential V
shaped groove in the bakelite base, just inside the alloy lip. The
base turned out to be 4 mm thick! I put new caps inside, 0.1uF
3.5KV "Custom" mica caps from Surplus Sales Nebraska. They
were the only type of the correct value that I could find that would
fit in the can. I re-potted the can with polyester resin( won't be
going back in there again!). The polyester also fills the V shaped
groove holding the base back on to the capacitor.
Other items in the photo are the Square electrolytic in the
cardboard box, also potted in with polyester( actually this is the
yoke coupling cap) so instead I put in a 10uF Solen Fast 630V non
electrolytic from Antique Electronics, so there will never be any
problems with that. There are also a couple of other electrolytics
that got repaired. Also in the background you can see the repainted
line oscillator and output trans. I think the casing of those is a
nickel/steel alloy. It was rubbed down, treated with rust convertor,
undercoated, rubbed down again with 1200 paper and sprayed with fine
silver lacquer.
Some tips on polyester resin if you use it: The correct proportion
of hardener is said to be 10 to 20 ml per litre, or 1ml per 100ml. It
is best to use the smaller amount, especially if you are filling a
volume with it. With an object like the can capacitor, or the one in
the cardboard box, the surface area to volume ratio is low. As the
resin catalyses it is exothermic, so in these size/shape objects it
can get quite hot suddenly as the temp builds up, speeding up the
process. So for this type of thing I find about 0.8 ml per 100 ml
resin is the best as it goes off a bit slower with less heat.

June 2002: The electroplating is now complete. The process I have
selected for this is "Electroless Nickel" This process
electroplates without a DC current, and electroplates down the inside
of holes and into corners. It has a beautiful metallic silver look to
it and is very suitable for complex shaped small parts, eg the bulb
sockets. All of the rust from each component was blasted off (not
polished). This leaves a satin surface, completely devoid of any rust
particles. You can see just how much rust there was in the
pre-restoration photo. As can be seen, this set has a myriad of
mechanical parts, each one treated as above, then a coat of
protective clear lacquer applied. Nickel's electrons are not
particularly sacrificial to steel, but on the other had the nickel
maintains an excellent surface, particularly if protected by lacquer
or clear enamel. I have been able to re-assemble the speaker. The
variable capacitor frame also got electroplated and reassembled
after cleaning the corrosion of all its components. It is important
that areas of metal work that are protectively clear lacquered, that
masking is used in the areas requiring earthing.
The yoke was cleaned and some insulation replaced and the yoke re-varnished.
The tube shields are restored, by rubbing down with 800 then 1200
grade parer. Treated with rust convertor. Undercoated with automotive
primer, rubbed down with 1200 paper, painted with automotive silver.
The aluminium tops were polished with 3M marine aluminium polish
prior to painting the other parts of the shield. Then the aluminium
cleaned with solvent to remove all traces of polish, then the whole
shield sprayed with topcoat clear to protect the aluminium and silver
paint too. The inner part of the shield was appropriately masked to
allow good electrical contact with the ring it mounts on to.


August, 2002: The chain for the radio tuning dial was
missing on my set, and I found some similar chain at a hobby shop.
Turns. Turns out that I could not stretch the steel chain enough to
make it fit the sprockets, so I figured out the exact dimensions of
it and am getting a local Jeweler to make it. Turns out these guys
only work with precious metals (wouldn't you know it) and it looks
like white gold would be better than silver in terms of its physical
properties, hardness etc and of course $$.
Turned on the set for the first time, a continuous crackle from
the speaker, I knew all the tubes and resistors were good. Quickly
traced it to the primary of the Audio opt transformer, The DC
resistance was 200 ohms too high and when a current passes through
it, it generated horrible noise, So I unstacked it and removed the
secondary winding and inspected one of the connections to the lead in
wires on the primary, it was ok. Then I removed the central cardboard
form from the middle of the winding to get at the other connection,
it too also ok! So with nothing left to lose I started to unwind the
primary from the inside layer. After only 1/3 a layer the wire fell
apart and I found a green spot of corrosion. Reconnected it after
that fixed up, and problem solved. I rewound the secondary back on
with replacement 0.63mm diameter wire, made a new
cardboard former for the center, and varnished it up after that, it's
still drying. So that should have solved that problem unless there
are more green spots waiting to give trouble! Then I can start the alignment
I've been doing quite a bit of work on the IF stages, trying to
figure out what the manufacturers intended, versus what I can do with
it. I've got some great sweep generators and RF sources. The way they
configured it is fairly restrictive on bandwidth, only about 1.8 to 2
MHz. That is when I best configure it with a sound frequency of 41.5
MHz and a center vision IF Frequency of 45MHz. On the other hand it
is possible to adjust it for a wider bandwidth( as there is plenty of
gain), to 2.4MHz bandwidth by re-assigning the vision frequency to
about 44,5Mz. One generator I have only puts out a signal with sound
and vision 4.5 MHz apart, but with your RF modulators I can tune any
value I like. On balance I will probably leave the frequencies as the
manufacturers intended, but I know on account of this, the
screen image will be "softer". Makes me realise how
expectations of a good television image must have changed a lot over
the latter 50 years of the last century, and now we take the
resolution for granted, like that which make the fine graphics
visible on our computer screens. However the American sets of the
time appear to have paid more attention to the bandwidth issue.
I've had some fun playing around with some different 5FP4's. In
general they have quite good images despite only 2.3KV on the anode.
The book says they are recommended for 4Kv and above. The advantage
they have over a 5AP4 or 5BP4 is that on highlights or over a range
of intensities they stay focused! Some I have, the beam centering is
a problem and can only just centre the image centred by moving the
yoke wrt focus coil. In one case I had to try a small DC current
through the frame coils to get a centered image. I've found that by
running the line stage at 1/2 our 625 line rate it locks up OK , with
good width and linearity, but of course 2 images side by side, but OK
for test purposes. I ended tying the anode of the 5FP4 to a
lower potential (150 volts) to the screen grid of one of the tubes,
V8. With this lowered the CRT was more sensitive to video signal and
had better contrast and easier to focus.
The IF in this set is really complex and difficult compared to any
I have worked on before. It's not just a matter of setting it up for
some characteristic with a sweep generator. The sound and vision
parts of it interact significantly and there is a fairly narrow set
of adjustment compromises which allow a combination of good vision,
good sound and lack of interference of sound in the vision and to a
lesser degree lack of interference of vision on sound quality. This
has all to be satisfactory with at least 25 to 30 volts PP video
signal at the tube cathode to get maximal contrast, all with a
sensible level of incoming vision and sound carrier. Each time
the vision circuit is touched the sound IF needs a small adjustment
too. In the end I concluded that the bandpass characteristic the
manufacturers intended was not the usual flat top response we are
used to. Accepting that, I found that after setting the response as
best possible on the sweep generator, that I merely adjusted the
tuned circuits for the best looking video signal with a multi-burst
test signal from my generator. It is possible on the screen to
resolve the 0.8 MHz and 1.8 MHz sinewaves but no more. The 2.8 and
3.8 MHz waves are not visible. Overall though, the signal looks good,
with very respectable square edged sync pulses etc. Then when I when
back and swept the IF the bandwidth comes out at about 1.4 MHz. If I
attempt the broaden the bandwidth the gain in the video drops so you
need more RF carrier input for the same contrast, then the vision
carrier which comes along with it( from my generator) becomes
excessive and interferes with the video. If I use a separate vision
carrier, I then have to reduce the sound signal and the S/N ratio in
the sound is poorer. So in effect it can all be made to work ok with
exact frequencies of 41.5MHz sound and 45MHz vision, if I accept that
the video bandwidth is not what I'm used to, and certainly not what a
5FP4 could support. But I suppose the transmissions in those days
were pretty "soft" anyway. In my set the height is only
just adequate, with all voltages correct, how is yours? I'd bet it
would have been better with a choke for the anode load in the frame
opt tube rather than that 10K resistor!

Have a look at this JPG of the screen image with a checkerboard,
625 line signal. Good contrast and brightness. The image is upside
down, as the yoke is rotated around. At the end of line scan the
bright bar is the picture getting involved in retrace time and the
linearity is poor on what is the left side of the image(if the yoke
was in the correct place). When I slow down the line stage to the
correct frequency the linearity is fine, and the width better. By
loosening the focus coil and adjusting it, I found I could centre the
beam on all my CRTs ok. Tuned out that extra accelerating electrode
in the 5FP4 is handy to adjust things so the gun probably behaves
very similarly to a 3/1. So the 5FP4 is an excellent substitute and
really the only option there is at all.

Here is a photo of a 405 line source after the problems have been fixed.

Here is a picture of the completed chassis with the 5FP4

The underside of the chassis |